MAX 9 Resumed Flying on 1/26/2024
#31
FlyerTalk Evangelist
Join Date: Dec 2006
Location: Pacific Northwest
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Posts: 16,856
#32
Join Date: Apr 2003
Location: SEA, NW/DL 1.6Million Miler
Programs: DL 1MM Annual Silver,AS 100K 22-24, AS 75K 15-21
Posts: 4,278
Does anyone know what will become of the aircraft? Will it eventually resume flying as part of AS fleet? Will it recertify to regain ETOPS?
Jiburi
Jiburi
#33
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#34
A FlyerTalk Posting Legend, Moderator, Information Desk, Ambassador, Alaska Airlines
Join Date: Dec 2006
Location: FAI
Programs: AS MVP Gold100K, AS 1MM, Maika`i Card, AGR, HH Gold, Hertz PC, Marriott Titanium LTG, CO, 7H, BA, 8E
Posts: 42,953
Been on 2 7M9 in the past week. One was a rescue flight when it was too cold in FAI for the E175 to operate.
#37
Join Date: Apr 2003
Location: SEA, NW/DL 1.6Million Miler
Programs: DL 1MM Annual Silver,AS 100K 22-24, AS 75K 15-21
Posts: 4,278
#38
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#39
Join Date: Apr 2018
Programs: Alaska Mileage Plan
Posts: 89
#40
Join Date: Mar 2023
Posts: 5
Next 7M9 glitch?
Today (AS30, PDX-JFK) the FAs could not get the piped-in boarding music to stop playing before takeoff. They had to disarm doors for maintenance to board. It appeared to be a 2 minute fix. Five hours of boarding music would definitely render the plane non-airworthy IMO….
#41
FlyerTalk Evangelist
Join Date: Dec 2006
Location: Pacific Northwest
Programs: UA Gold 1MM, AS 75k, AA Plat, Bonvoyed Gold, Honors Dia, Hyatt Explorer, IHG Plat, ...
Posts: 16,856
Today (AS30, PDX-JFK) the FAs could not get the piped-in boarding music to stop playing before takeoff. They had to disarm doors for maintenance to board. It appeared to be a 2 minute fix. Five hours of boarding music would definitely render the plane non-airworthy IMO….
Ground the fleet NOW!
#42
Join Date: Apr 2003
Programs: B6 Mosaic, Bonvoy LT Titanium (x SPG LT), IHG Spire, UA Silver
Posts: 5,848
Today (AS30, PDX-JFK) the FAs could not get the piped-in boarding music to stop playing before takeoff. They had to disarm doors for maintenance to board. It appeared to be a 2 minute fix. Five hours of boarding music would definitely render the plane non-airworthy IMO….
#43
Join Date: Aug 2015
Location: SFO
Programs: AS 75K (OW), SK Silver (*A), UR, MR
Posts: 3,347
Meanwhile,
Investigators say they confirmed pilots’ account of a rudder-control failure on a Boeing Max jet
https://www.alaskasnewssource.com/20...outputType=amp
Investigators say they confirmed pilots’ account of a rudder-control failure on a Boeing Max jet
https://www.alaskasnewssource.com/20...outputType=amp
#44
Join Date: Apr 2009
Location: YYF/YLW
Programs: AA, DL, AS, VA, WS Silver
Posts: 5,951
Meanwhile,
Investigators say they confirmed pilots’ account of a rudder-control failure on a Boeing Max jet
https://www.alaskasnewssource.com/20...outputType=amp
Investigators say they confirmed pilots’ account of a rudder-control failure on a Boeing Max jet
https://www.alaskasnewssource.com/20...outputType=amp
Boeing said this is the only rudder-response issue reported on a Max, although two similar incidents happened in 2019 with an earlier model of the 737 called NG or next generation, which has the same rudder-pedal system.
#45
Join Date: Jul 2000
Location: Kirkland, WA
Posts: 71
Just got an alert for this NYTimes story. Not great PR for Alaska.
"A day before the door plug blew out of an Alaska Airlines flight on Jan. 5, engineers and technicians for the airline were so concerned about the mounting evidence of a problem that they wanted the plane to come out of service the next evening and undergo maintenance, interviews and documents show.
But the airline chose to keep the plane, a Boeing 737 Max 9, in service on Jan. 5 with some restrictions, carrying passengers until it completed three flights that were scheduled to end that night in Portland, Ore., the site of one of the airline’s maintenance facilities."
"A day before the door plug blew out of an Alaska Airlines flight on Jan. 5, engineers and technicians for the airline were so concerned about the mounting evidence of a problem that they wanted the plane to come out of service the next evening and undergo maintenance, interviews and documents show.
But the airline chose to keep the plane, a Boeing 737 Max 9, in service on Jan. 5 with some restrictions, carrying passengers until it completed three flights that were scheduled to end that night in Portland, Ore., the site of one of the airline’s maintenance facilities."