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MAX 9 Resumed Flying on 1/26/2024

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Old Feb 7, 2024, 2:39 pm
  #31  
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Originally Posted by jhoehn
I would think that after inspection seat 26A would be the safest spot on a Max9?
I'll take row 2, please.
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Old Feb 7, 2024, 4:39 pm
  #32  
 
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Does anyone know what will become of the aircraft? Will it eventually resume flying as part of AS fleet? Will it recertify to regain ETOPS?

Jiburi
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Old Feb 7, 2024, 5:04 pm
  #33  
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Originally Posted by jiburi
Does anyone know what will become of the aircraft? Will it eventually resume flying as part of AS fleet? Will it recertify to regain ETOPS?

Jiburi

I’d be shocked if N704AL wouldn’t rejoin the fleet.
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Old Feb 8, 2024, 8:55 pm
  #34  
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Been on 2 7M9 in the past week. One was a rescue flight when it was too cold in FAI for the E175 to operate.
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Old Feb 14, 2024, 4:37 am
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Just boarded AS 465 from TPA-SEA. App is still showing 737-9 MAX but actual plane is 737-900.
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Old Feb 14, 2024, 10:27 am
  #36  
 
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The flight status webpage for yesterday's ORD-SFO said 9 MAX, as did my reservation. The aircraft really was a 9 MAX.
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Old Feb 14, 2024, 9:08 pm
  #37  
 
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Originally Posted by notquiteaff
I’d be shocked if N704AL wouldn’t rejoin the fleet.
FlightAware hasn’t shown any flight activity since the incident…. I would at least think N704AL would be ferried somewhere by now…

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Old Feb 14, 2024, 9:24 pm
  #38  
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Originally Posted by jiburi
FlightAware hasn’t shown any flight activity since the incident…. I would at least think N704AL would be ferried somewhere by now…
Can’t they fix it in Portland?
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Old Feb 16, 2024, 7:37 am
  #39  
 
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Originally Posted by notquiteaff
Can’t they fix it in Portland?
From what the NTSB said, there was a lot of interior cabin damage. Might have to ferry it back to a facility that does cabin installations (not sure if PDX ever does them).
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Old Feb 19, 2024, 10:25 am
  #40  
 
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Next 7M9 glitch?

Today (AS30, PDX-JFK) the FAs could not get the piped-in boarding music to stop playing before takeoff. They had to disarm doors for maintenance to board. It appeared to be a 2 minute fix. Five hours of boarding music would definitely render the plane non-airworthy IMO….
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Old Feb 20, 2024, 5:11 pm
  #41  
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Originally Posted by SalmonThirtyRamblin
Today (AS30, PDX-JFK) the FAs could not get the piped-in boarding music to stop playing before takeoff. They had to disarm doors for maintenance to board. It appeared to be a 2 minute fix. Five hours of boarding music would definitely render the plane non-airworthy IMO….

Ground the fleet NOW!
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Old Feb 20, 2024, 6:32 pm
  #42  
 
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Originally Posted by SalmonThirtyRamblin
Today (AS30, PDX-JFK) the FAs could not get the piped-in boarding music to stop playing before takeoff. They had to disarm doors for maintenance to board. It appeared to be a 2 minute fix. Five hours of boarding music would definitely render the plane non-airworthy IMO….
The white noise machine activated by tossing the plug door out of the plane could have fixed that problem
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Old Mar 7, 2024, 6:44 pm
  #43  
 
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Meanwhile,

Investigators say they confirmed pilots’ account of a rudder-control failure on a Boeing Max jet
https://www.alaskasnewssource.com/20...outputType=amp
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Old Mar 7, 2024, 10:54 pm
  #44  
 
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Originally Posted by vanillabean
Meanwhile,

Investigators say they confirmed pilots’ account of a rudder-control failure on a Boeing Max jet
https://www.alaskasnewssource.com/20...outputType=amp
Although (from that article) it appears to be key context that this is not a Max-specific design:
Boeing said this is the only rudder-response issue reported on a Max, although two similar incidents happened in 2019 with an earlier model of the 737 called NG or next generation, which has the same rudder-pedal system.
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Old Mar 12, 2024, 3:06 pm
  #45  
 
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Just got an alert for this NYTimes story. Not great PR for Alaska.

"A day before the door plug blew out of an Alaska Airlines flight on Jan. 5, engineers and technicians for the airline were so concerned about the mounting evidence of a problem that they wanted the plane to come out of service the next evening and undergo maintenance, interviews and documents show.

But the airline chose to keep the plane, a Boeing 737 Max 9, in service on Jan. 5 with some restrictions, carrying passengers until it completed three flights that were scheduled to end that night in Portland, Ore., the site of one of the airline’s maintenance facilities."
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